LMM: LMM with 222,000 tear down rebuild

S Phinney

Active member
Aug 15, 2008
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You need a better gauge that reads .0001 +-, not the .0005 +- you are using if you really want the best readings on the bores. You will have a hard time making sure bearings are matched to the mains or rods without it.

Assuming decent accuracy of the gauge as well, by the time you hone, you will be .001-.002 above what you have now and that's if the machine shop will take the time to really get you the specified clearances you want. She's gunna be loose on that ptw clearance and close to service limit
If the walls look good a new cross hatch can be done and only gain a half a thousandth if the shop has the right tools and know what they are doing. .

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malibu795

misspeelleerr
Apr 28, 2007
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If the walls look good a new cross hatch can be done and only gain a half a thousandth if the shop has the right tools and know what they are doing. .

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Only 3 shops close to me that could do that.. all are week out lead tines. And 2.5 hours one way...
D&J performance in Cambridge ohio
Fleece
And guys Danville uses
 

PureHybrid

Isuzu Shakes IT
Feb 15, 2012
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So are you honing it yourself?

Try Galen at the Performance Shop in Newark. He might be too busy but it's worth a shot, does good work. Tell him Moose sent you

And fwiw I never bother buying a low reading bore gauge anyway, they are too inaccurate for my taste. They can give you a good quick look at how a cylinder is worn, but I prefer snap gauges.
 

malibu795

misspeelleerr
Apr 28, 2007
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So are you honing it yourself?

Try Galen at the Performance Shop in Newark. He might be too busy but it's worth a shot, does good work. Tell him Moose sent you

I know if i dont hone it it will take longer to seat.. i also dont have anything that will go through thw induction hardened top part
I don't if he could knock it out quickly as in same/next day.

i currently got ~5 weeks till labor day, And 17 weeks till Thanksgiving
Stuff starts slowing down after Thanksgiving......
 

Chevy1925

don't know sh!t about IFS
Staff member
Oct 21, 2009
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If the walls look good a new cross hatch can be done and only gain a half a thousandth if the shop has the right tools and know what they are doing. .

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That's assuming your cyl is still semi square as well.
 

Stingpuller

The Pusher Man
Jan 11, 2007
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Your motor

I would bead hone it not worry about coating the pistons and roll! Under the heat you run you want a loose on the ptw clearance.
 

malibu795

misspeelleerr
Apr 28, 2007
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Grove on camshaft is 5*2.5mm grove, on the cam gear is 5*5mm was given a 5*5*16mm key. Cut in 1/2 file to fit..Problem fixed
13626964_10209108759369687_2664471892166710403_n.jpg
 

malibu795

misspeelleerr
Apr 28, 2007
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And here I thought Hamilton knew what they were doing. Did they give you a key or someone else?

Hamilton gave me 2 5mm holes for OEM press fit pins fleece cut a 5mm keyway and put a 5*5*16mm key in it.

Honestly idk until little bit ago.. had cam installed with gear off.. so i put the key in the gear to slide it on.. and found out

The LMM cam i had keyed is exactly same thing 5*7mm keyway with a 5*5mm key fleece did that one as well
 

malibu795

misspeelleerr
Apr 28, 2007
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Forgot to post ring gaps
Took a piston and shoved them down until top of wrist pin was flush with deck

Old
1st .023"
2nd .024

New rings
1st .018
2nd .024

Both ring sets where mahle #41909

Id Say the .023" gap on the top ring allowed the carbon/gum up of the secondary causeing it to stick and increase blow by
 

malibu795

misspeelleerr
Apr 28, 2007
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So do you think was causing the lack of power? I really don't think the ring gap is

With .023 to and .024 bottem and how much carbon/gummed up the secondary was.. that could easily keep the secondary from tracking along the wall and naturally increase blow by

Id saw it definitely contributed to los of power and blow bye
 

Stingpuller

The Pusher Man
Jan 11, 2007
2,019
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Really

How do you figure? He has tried new with bad results. I will say it again, I have NEVER seen a loose motor be a problem. Tight and you WILL have problems. His deal is much like a marine motor. Heat for a very long time. He needs to figure out his ring seal is the only thing I would worry about. That top ring gap he had would be the cause of the problem. I would be scared to run it that tight with the heat he makes. That's just me.
 

IOWA LLY

Yes, its really me
Feb 23, 2007
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Jeff, I'm a little confused with what your saying? Are you saying you wouldn't run his ring end gap that tight with the heat he's making? Or the ptw clearance that tight? I'm pretty sure I'm following you but I want to make sure.

John, what do you think the cause of Adam's failure was? Maybe failure is the wrong word... His "issue" I guess would be a better description.

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malibu795

misspeelleerr
Apr 28, 2007
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Issues i had.
Loss of HP as indicated by dyno and drop in grade speed
Loss of MPG as i dropped ~2mpg
300-360psi range with a compression test.
Substantial increase in blow bye

What did i find.
70k increased ring gap from .017 to .023
Gummed/carboned up second ring making to difficult to move
 

Stingpuller

The Pusher Man
Jan 11, 2007
2,019
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Motor

I personally would run (start) around .024 or so and run the pistons on the loose side. You would have to have some major piston rock to effect ring seal that bad. Adam I don't remember but do you run head studs? I have seen them affect ring seal when you don't use a TQ to hone the block after studs are installed. The top of the bore will move were the studs/holes are in the bore.
 

malibu795

misspeelleerr
Apr 28, 2007
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Since ivr yet to lift heads with the LML Head bolts and dont intend to run more than stock fuel, (still have a stock transmission) i haven't done anything with/for head studs
When fleece did the block, specifically ask not to TQ plate hone as i have no intention of running studs, and dont think head bolts could bring the walls back into a circle

Might head stud the block i build this winter... Cross that bridge when i get there