Wanted to extend a big thanks to Dan@PPE along with his awesome mechanics! Also wanted to say thanks to Rob@ATP as well for tuning!
Here's what took place:
The Rear main seal on the truck started leaking the day after I picked the truck up from PPE, not that big a deal, I kept a close eye on the oil and put about 20k on the new motor with that leak. Finally was able to get the truck back to PPE to address the RMS leak. I also knew of another issue because Rob caught it in my data logs, the CP3 was not maintaining fuel rail pressure in high demand situations.
I spoke with Dan to get the truck in and I wanted to put a new LBZ CP3 in the valley and a lift pump, to solve the fueling issues while the motor was out having the RMS fixed.
Dropped the truck off, PPE pulled the motor and later that day Dan called me and informed me that my stock IHI was a ticking time bomb with 1/4" shaft play.
I was not expecting this and I had to pull together all my resources, because I didn't want a stock turbo anyway.
Well I found the money and was able to give the go ahead to have PPE put in a GT4088r.
I got the truck back and it was a little funky because the FPR was off because of the LBZ pump. I had the truck tuned in Cali good enough to get home to NM, but was still not happy with the way it was performing.
I picked up the phone Monday morning and called ATP for tunes they had them to me by Monday night.
Tuesday I loaded them up and went for a drive on my max effort tune! Holy cow is this truck something now it performs effortlessly, and is very quiet! Turbo is not laggy at all and the truck accelerates with ease!
This is the happiest I've been since I've owned the truck!
So again a big Thanks to PPE for great work on the truck, and to Rob@ATP for the great tunes!
Sent from my iPhone using Tapatalk
Here's what took place:
The Rear main seal on the truck started leaking the day after I picked the truck up from PPE, not that big a deal, I kept a close eye on the oil and put about 20k on the new motor with that leak. Finally was able to get the truck back to PPE to address the RMS leak. I also knew of another issue because Rob caught it in my data logs, the CP3 was not maintaining fuel rail pressure in high demand situations.
I spoke with Dan to get the truck in and I wanted to put a new LBZ CP3 in the valley and a lift pump, to solve the fueling issues while the motor was out having the RMS fixed.
Dropped the truck off, PPE pulled the motor and later that day Dan called me and informed me that my stock IHI was a ticking time bomb with 1/4" shaft play.
I was not expecting this and I had to pull together all my resources, because I didn't want a stock turbo anyway.
Well I found the money and was able to give the go ahead to have PPE put in a GT4088r.
I got the truck back and it was a little funky because the FPR was off because of the LBZ pump. I had the truck tuned in Cali good enough to get home to NM, but was still not happy with the way it was performing.
I picked up the phone Monday morning and called ATP for tunes they had them to me by Monday night.
Tuesday I loaded them up and went for a drive on my max effort tune! Holy cow is this truck something now it performs effortlessly, and is very quiet! Turbo is not laggy at all and the truck accelerates with ease!
This is the happiest I've been since I've owned the truck!
So again a big Thanks to PPE for great work on the truck, and to Rob@ATP for the great tunes!
Sent from my iPhone using Tapatalk